Corresponding author: Vladimir P. Povarov ( povarovvp@nvnpp1.rosenergoatom.ru ) Academic editor: Yury Kazansky
© 2019 Vladimir P. Povarov, Anatoly I. Fedorov, Sergey L. Vitkovsky.
This is an open access article distributed under the terms of the Creative Commons Attribution License (CC BY 4.0), which permits unrestricted use, distribution, and reproduction in any medium, provided the original author and source are credited.
Citation:
Povarov VP, Fedorov AI, Vitkovsky SL (2019) Some aspects of the VVER-440 reactor plant life re-extension: a case study of the Novovoronezh NPP Unit 4. Nuclear Energy and Technology 5(3): 249-256. https://doi.org/10.3897/nucet.5.46380
|
The re-modernization of Unit 4 at the Novovoronezh NPP (Novovoronezh-4) made it possible to take a new approach to the problem of extending the VVER-440 reactor plant life and operation. The authors analyze the existing problems of the VVER-440/179 power unit, showing possible solutions to the identified shortcomings and the final state of the updated power unit. Modernization works significantly expanded the range of design-basis accidents from the primary coolant leak from an opening (DN = 100 mm) to the maximum possible, associated with a rupture of the main circulation pipelines (MCP) (DN = 500 mm). A unique experience was gained in using the safety systems of Unit 3, which was finally shutdown for decommissioning, to increase reliability and provide additional redundancy for the safety systems of Unit 4.
The results of the performed works showed the correctness of the adopted concept of re-extending the service life of Unit 4 and ensured its compliance with the modern safety requirements in nuclear power engineering, including as it relates to the safety impact of the first-level probabilistic safety analysis model (PSA-1) for internal initiating events.
Life re-extension, VVER-440, V-179, fluence, radiation embrittlement, safety systems, reactor vessel annealing
In 2019, the Novovoronezh nuclear power plant (NvNPP) celebrates the 55th anniversary of its first power unit commissioning. During this time, the entire VVER line from the VVER-210 to the VVER-1200 was tested at the NPP. The authors attempt to summarize the problems associated with NvNPP Unit 4 life re-extension, showing possible solutions to complex technical problems and analyzing the gained experience, which should be necessarily replicated for all domestic VVER designs to extend their service life up to 60 years.
The first conceptual studies related to water-cooled power reactor plants started in the USSR as early as in 1954 (the year of the launch of the world’s first nuclear power plant with an AM-1 uranium-graphite reactor) and were based on the submarine reactor pilot projects. In September 1955, an updated specification was issued for the VVER reactor, and in 1957, the NvNPP construction began. The entire start-up process of the first NvNPP power unit with a VVER-210-type reactor took less than four months: the physical start-up took place on September 8, the power start-up was on September 30, and the commissioning was on December 27, 1964. The theoretical and practical study of the VVER technology at the NvNPP led to the commissioning of Unit 2 with a capacity of 365 MW (VVER-365) in 1969 and Unit 3 with a VVER-440/179 reactor in 1971, which gave rise to a full-scale series of nuclear power units that have spread not only in the territory of the USSR but also in many European countries. As result of the sequential commissioning of Unit 4 with a VVER-440 reactor in 1972 and Unit 5 (VVER-1000) in 1980, the NvNPP reached a total capacity that allowed it to be considered the most powerful nuclear power plant in Europe at that time interval. In 2016, the Generation 3+ VVER-1200 power unit was started up. Thus, currently, the NvNPP has the following configuration: the VVER-210 (Unit 1) and the VVER-365 (Unit 2) were decommissioned in 1984 and 1990, respectively; the VVER-440 (Units 3 and 4) underwent the service life extension procedure in 2001 and 2002, respectively, for 15 years; in 2017, Unit 3 was shut down for decommissioning and Unit 4 underwent a repeated procedure for extending its service life for another 15 years (
In January 1966, based on the technical specifications, OKB Gidropress developed a technical design of the VVER-440 reactor for typical nuclear power plants with two units of 400 MW each, and it was decided to use the VVER-440 (V-179) design for Units 3 and 4. For serial power units of NPPs with VVER-440 being built in our country and abroad, a new reactor design, V-230, was developed, which took into account the requirements of foreign customers in addition to the domestic ones (
The VVER-440/179 reactor design was developed on the basis of the accumulated experience in designing, manufacturing, installing, commissioning, and operating the VVER-210 and VVER-365 reactor plants previously developed by OKB Gidropress and operated at the NvNPP site. At the same time, a number of design solutions met the recommendations of the IAEA INSAG-5 Report for future NPPs, published only in 1992, the main ones being as follows:
As the maximum design-basis accident, a leak of the DN100 pipeline with a DN32 restrictive insert was postulated, and the core damage frequency (CDF) was assumed to be 1.08·10–3 reactor-years–1, which corresponded to the safety standards and regulations of the 60s.
The VVER-440 design was based on the concept that by ensuring the high quality of the reactor plant equipment and components, their efficient operation and condition monitoring of the metal and equipment welds, it is possible to avoid their heavy damage and, therefore, eliminate the possibility of a severe accident.
The work on extending the service life of Units 3 and 4 had begun long before they expired their design life of 30 years, assuming the following sequence:
The life of the entire NPP power unit was determined by the life of the reactor vessel as the largest “irreplaceable” component (
A detailed analysis of the accumulated factual material (templates) conducted by qualified material specialists and performance calculations showed that the reactor vessels of Novovoronezh-3 and -4 meet the brittle strength criteria in normal operation and emergency modes for an additional 15-year period (
Works performed on Novovoronezh-3 and -4 in order to extend the lives of their vessels.
Unit 3 | Year | Unit 4 |
---|---|---|
Reactor vessel annealing. Mode: T = 430 ºС, t = 150 h | 1987 | |
Selecting templates from Weld 4 and base metal of the reactor vessel shell | 1991 | Selecting templates from Weld 4 and base metal of the reactor vessel shell |
Reactor vessel annealing. Mode: T = 475±15 ºС, t = 100 h | Reactor vessel annealing. Mode: T = 475±10 ºС, t = 150 h | |
Selecting templates from Weld 4 and base metal of the reactor vessel shell | Selecting templates from Weld 4 and base metal of the reactor vessel shell | |
Selecting templates from Weld 4 and base metal of the reactor vessel shell | 1995 | Selecting templates from Weld 4 and base metal of the reactor vessel shell |
Selecting templates from Weld 4 and base metal of the reactor vessel shell | 2003 |
In order to extend the service life of Units 3 and 4 up to 45 years, the following measures were developed to improve their safety:
The following results were achieved:
The results of the first service life extension (SLE) of Novovoronezh-3 and -4 clearly showed that it would be technically possible to further extend their service lives. At the same time, the condition of the components of Unit 3 (upper unit, reactor vessel, steam generators, etc.) required significantly more work during the SLE as compared to those of Unit 4 (
The Scientific and Technical Council of OJSC Concern Rosenergoatom, by its decision of 06.29.2012, recommended that Unit 3 be shut down at the end of its 45-year service life and a set of documents be developed to justify the expediency of extending the service life of Unit 4 over 45 years, taking into account (
The main problem was the ECCS composition that did not meet the requirements of the current regulatory documents in the field of atomic energy use, in particular, when the full range of loss of coolant accidents (up to LOCA – DN 500) is considered. Therefore, one of the main goals in the concept of improving the level of safety during Unit 4 service life extension up to 60 years was to expand the range of design-basis accidents up to the MCP (DN 500) rupture. For this end, the following technical solutions were proposed:
In general, according to the project of extending the life of Novovoronezh-4 over 45 years, more than 40 measures have been implemented.
The concept of re-extending the service life of Unit 4 provided for a safety level increase by expanding the spectrum of design-basis accidents up to the MCP (DN = 500 mm) rupture. This goal was achieved by creating four channels of the high pressure emergency core cooling system. Two channels are formed by 4EFP-1, -2 and 4EFP-5, -6 pumps and two additional channels are formed by 3EFP-1, -2 and 3EFP-5, -6 pumps (Fig.
The existing 3EFP-3,4 have been transferred to the controls of beyond-design-basis accidents (BDBA). These pumping units are supposed to be used to perform safety functions (core cooling) in the event of extreme external influences causing the failure of existing design tools (as redundant 3,4APN-1, -2, -5, -6).
The estimates made by OKB Gidropress for an accident with the “MCP (DN = 500 mm) break” initiating event indicate that the temperature of the fuel elements does not exceed 800 °C, i.e., depressurization of initially hermetic fuel elements in this accident is not predicted.
The system is designed as an emergency one to have no single point of failure and ensure the supply of boric acid solution from T-8/3,4 tanks in all design-basis accident modes associated with the primary leak. The emergency core cooling system (passive ECCS) comprises four hydro-accumulators (two channels of two ECCS accumulator tanks), while the low pressure emergency core cooling system (LP ECCS) uses newly mounted low pressure safety injection pumps EFP-1, -2, -3 (three channels with one pump in each) (Fig.
After the service life of Unit 4 was extended to 45 years, as a result of modernization, the containment was equipped with a jet-vortex condenser (4JVC), which made it possible to increase the range of design-basis accidents before the event associated with the pipeline (DN = 100 mm) rupture. However, the expert assessment showed that the occurrence of an accident associated with a double-ended guillotine MCP (DN = 500 mm) break will lead to an excess of the maximum design pressure in the containment. In order to reduce the pressure during a hypothetical accident, the sealed compartments of the two units were combined by a jumper in the form of three steel communication pipelines (DN = 1620 mm) with a total area of S = 6,18м² for the gas flow to pass. In doing so, all the requirements of modern regulatory documentation were taken into account, and the complete gas medium flow through the steel communication pipelines during a design-basis accident was ensured, including compliance with seismic resistance standards (Fig.
The spray system’s function is to maintain the temperature of the boron solution in the tank T-8/3,4 in the range from 55 to 65 °C in all modes when emergency reactor feeding from the tank T-8/3,4 may be required.
Reactor vessel. To make a decision on Unit 4 re-modernization, one of the main issues was a correct and complete performance assessment of the reactor vessel exposed to severe radiation during operation.
Assessments of the neutron fluence on the reactor vessel walls made by the OKB Gidropress specialists showed the following:
The main factor in determining the the reactor vessel life is its justification for brittle fracture resistance (BFR) (
To extend the service life of the reactor vessel of Novovoronezh-4 over 45 years, a second recovery annealing was carried out at a temperature of ± 15 °С for 150 hours. The justification for extending the service life of the reactor vessel of Unit 4 over 45 years took into account the recovery of metal properties in the areas of guaranteed annealing (at a temperature of 475 ± 15 °С) and temperature gradient (420–460 °С). The novelty and distinctive feature of the second reactor vessel annealing of Unit 4 from the beginning of its operation is that, in addition to Weld 4, the core shell was subjected to annealing with a total annealing zone of 2340 mm (from 282 mm below the weld axis to 2058 mm above Weld 4 axis). The decision to expand the annealing zone was made due to the fact that the fluence that can be accumulated during operation up to 60 years on the core shell will exceed 3.0·1024м–2 (Е > 0.5 MeV), to which the workability of steel 15H2MFA is substantiated. After the reactor vessel was re-annealed, positive results were obtained in extending the reactor vessel life up to 60 years and guaranteed values of the strength properties and critical brittleness temperature were determined for the reactor vessel metal, primarily for Weld 4 as the most critical reactor component with respect to brittle fracture (
The greatest danger for the reactor vessel brittle fracture resistance is represented by emergency ECCS actuation conditions – they are decisive in terms of the reactor vessel integrity and service life. Welds 4 and 5 as well as the upper shell are the most dangerous (decisive) components of the reactor vessel irradiated part in terms of its brittle fracture resistance. The nozzle zone is the decisive component of the reactor vessel non-irradiated in terms of its brittle fracture resistance. Therefore, in the course of modernization, water heating was implemented in the ECCS accumulator tanks. Maintaining the water temperature in the ECCS at or above 55 °C will reduce the thermal effects on the cylindrical part of the reactor vessel when the system is actuated in emergency situations.
The calculation results documented in 179-R-260 “Analysis of the NvNPP Unit 4 reactor vessel radiation durability” clearly indicate that the reactor vessel radiation durability is ensured until the end of the design life (
The analysis of the experience in operating the parts of the main joint seal assembly and other internals showed a high level of reliability. There were no failures that would lead to the reactor shutdown during operation. The service life of the reactor vessel and internals is longer than the design period due to the implemented measures to ensure the reactor vessel radiation durability beyond the design life, including annealing of Weld 4 metal and the base metal of the upper and middle shells during PPM-2018.
The steam generators of NvNPP Unit 4 have been in operation since 1972. An analysis of their operating experience has shown that the steam generators are highly reliable: no systematic failures have been identified, which would indicate a low quality of manufacture or installation of the equipment, its significant wear or problems with maintenance and personnel actions during operation.
The condition of the heat exchange tubes ensures that the SGs are operational for the planned period of 60 years subject to compliance with the requirements for operating SGs and, in particular, for maintaining the secondary circuit water chemistry (
In justification of the strength of the SG components, calculations were made for an extended list of modes, including both modes with normal operating conditions (NOC), anticipated operational occurrences (AOO) and emergency situations (ES) as well as a new list of modes for the new configuration of the power unit. The calculations confirmed that the geometrical dimensions of the main SG components do not exceed those adopted in the design, and the stresses from the internal pressure and other loads in the calculated components do not exceed the admissible ones (
The calculated SG component static and cyclic strengths showed that all the components satisfy the requirements (
The general technical condition of Unit 4 steam generators, the base metal and the metal of the heat exchange tubes as well as the number of plugged tubes in each steam generator (see Table
The number of plugged tubes in the steam generators does not exceed 5% of the total number of SG heat exchange tubes.
Condition of Unit 4 Steam Generators.
Parameter | Steam generator | |||||
---|---|---|---|---|---|---|
SG-1 | SG-2 | SG-3 | SG-4 | SG-5 | SG-6 | |
Plugged tubes, pcs | 117 | 111 | 61 | 128 | 169 | 205 |
Plugged tubes, % | 2.11 | 2.00 | 1.10 | 2.31 | 3.05 | 3.70 |
Conditions of fuel rods and the core during a maximum design-basis accident. The results of the thermal-hydraulic analysis of the “MCP (DN = 500 mm) break” accident initiating event for Unit 4 show that the temperature of the fuel element claddings does not exceed 800 °C. The changes in the reactor coolant parameters and the operating conditions of the fuel rods during the accident in question can be considered qualitatively coinciding with the propagation of a similar accident in the VVER-440/ 213 reactor, which also confirms the absence of plastic deformations of the fuel claddings.
Thus, it is shown that the modern configuration of security systems allows for core cooling in the considered initiating event. In order to expand the range of design-basis accidents up to the MCP (DN = 500 mm) break, in addition to upgrading the safety injection system described above, it is necessary to ensure the integrity of the existing fourth physical barrier, i.e. reactor containment and heat removal to the final absorber. This goal is achieved by combining the sealed compartments of Units 3 and 4. At the same time, the pressure in the reactor containment at the initial stage of the MCP break is limited not only by the increased containment volume but also by the operation of two JVCs. At subsequent stages, steam condensation in the sealed compartments and heat removal occurs while the spray systems of Units 3 and 4 are working.
Justification of seismic resistance of the reactor equipment and pipelines During the initial reactor life extension for Units 3 and 4 no calculations were made to verify the seismic resistance of the equipment and pipelines, since the intensity of the maximum design earthquake for the NvNPP site was estimated at that time to be 4.5 on the MSK-64 scale. For this level of seismic impacts, resistance testing is allowed to be carried out not in strict compliance with the standards for strength calculation of power unit equipment and pipelines (
The experience of extending the reactor life of Unit 5 showed that, at the present stage, Rostekhnadzor requires the seismic resistance to be justified regardless of the site location. Since the NvNPP location is not seismically active, the quality of the monitoring network can be assessed by its ability to record local industrial explosions and earthquakes from remote seismic zones.
The calculated effects for the verification estimates of the seismic stability of Unit 4 facilities (intensity 6 on the MSK-64 scale, acceleration 0.036 g and corresponding reaction spectra and accelerograms) are determined by the deterministic (scenario) method and conservatively attributed to the effects of the MDE level (maximum design earthquake).
Similarly, since it is impossible to perform a comprehensive probabilistic seismic hazard analysis for the NvNPP site, seismic effects of the DE level are proposed in the following terms: 1 point lower for intensity (i.e. 4 on the MSK-64 scale) and two times lower for acceleration (i.e. 0.018 g).
The analysis of design-basis accidents shows that, when any initial events of design-basis accidents occur at Unit 4, the acceptance criteria and, accordingly, the design limits adopted for design-basis accidents are not violated. In accordance with the main provisions of the “Concept of re-extending the life of Unit 4 at the Novovoronezh NPP КНС-265К (04-08) 2012, Rosenergoatom JSC, 2012”, the following goals were achieved:
As a result of the comprehensive modernization, the safety level of Unit 4 was increased due to the expansion of the range of design-basis accidents up to the MCP (DN = 500 mm) break. To achieve this goal, more than 40 measures have been implemented (for example, a backup control panel was installed, the safety control systems were replaced with modern ones, etc.).
After the modernization, the active systems comply with the requirements of the single-failure and independence principles according to (
According to the results of the probabilistic safety analysis (PSA), it can be concluded that the frequency of the limiting accidental release does not exceed 4,0·10–7 1/year. In accordance with (
The estimates obtained are close to the target and indicate that the design of Novovoronezh-4, taking into account the modernization measures, meets the most advanced requirements for ensuring public safety, while expanding the spectrum of design-basis accidents, increases its resistance to any external natural and man-made impacts declared in the Concept of re-extending the life of Unit 4.